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Northwest Pipeline LLC Notice Detail

Northwest Pipeline LLC


NOTICE # 22-123
Rangely-Vernal Cut Out Deficiency posted on Aug 12 2022 1:10PM

TSP Name:  Northwest Pipeline LLC     TSP:  67977322

Critical:  Y
Notice Stat Desc:  INITIATE
Notice Type Desc:  CURTAILMENT
Post D/T:  08/12/2022 1:08 PM MCT
Notice Eff D/T:  08/12/2022 1:08 PM MCT
Notice End D/T:  
Reqrd Rsp Desc:  No response required
Rsp D/T:  

Notice ID:  22-123
Prior Notice:  
Subject:  Rangely-Vernal Cut Out Deficiency

Notice Text:

As part of Northwest’s scheduled maintenance, pipeline

recoating between the Vernal and Rangely compressors is

currently taking place. During this time an anomaly was

discovered and a cutout between the two compressors will be

required.

 

The cutout is scheduled to take place on August 20, 2022.

Northwest will not be able to schedule nominations that net

greater than 162,000 Dth/d southbound through the Vernal

compressor or 155,500 Dth/d northbound through the Rangely

compressor. Current nominations for gas day August 12 are

approximately 220,686 Dth/d north through Rangely. Northwest

will mitigate volumes to the highest extent possible.

 

If the primary scheduled quantities for gas day August 20

exceed the operationally available capacity of 162,000 Dth/d

south through Vernal or 155,500 Dth/d north through Rangely, or

what Northwest is unable to mitigate, Northwest will give

notice of a Deficiency Period based on the Vernal compressor

southbound design capacity of 324,000 Dth/d and the Rangely

compressor northbound design capacity of 311,000 Dth/d.

 

If you have any questions, please call your Commercial Services

Representative or the hotline at 713-215-6301.